Flight #5
Conducted 07/04/2012 -
In our quest to lower the
oil temps, we discovered that the deflector installed just forward of the oil
cooler exit was not built correctly. The only depiction we had for his
deflector showed it only from the side, and thus did not indicate that the
deflector needed sides itself. We built a new deflector (with sides this
time) and stuck it on over the top of the existing one with RTV. We also
rigged up the next pressure test by installing pitot lines on both the top and
bottom of the oil cooler, and installing yet another set of valves and tees in
order to check the pressure drop across the oil cooler.
The temps in MN had been
much like the rest of the country, Hot. While it does make for a good
environment to test oil cooling, it's miserable for working on the plane or even
flying. We decided we would make the next test flight early in the morning
to at least make it tolerable to fly. So at the not so early morning hour
of 8am we arrived at the airport to conduct flight 5. John's flight report
is below:
I set up everything in
advance. The laptop, camcorder, radios, pitot valves, all ready to go
before I even climbed in. The engine again fired up and idled nicely, and I
quickly made my way for runway 13, contacting STC ground on the roll through the
ramp area. I got to the runup area and wasted no time performing my runup.
I took the runway with the oil temp at 147F, and quickly put 4TF back in the
air.
After leveling off, oil
temps had risen to 210F. I settled the power down to 20/20 and kept an eye
on the oil temp as it settled in at 215-217. I checked the pressure
reading at the oil cooler exit, it read static (0 an the ASI). I checked the
oil cooler inlet pressure, which read 85--90 Kts on the ASI, or approximately
4.75-5.25" H2O. I was pleased with the pressure differential across the
cooler, so I continued with the oft-interrupted Protocol 3 fight test card.
This involved adjusting power settings and leaning the fuel flow at each power
setting to determine if the engine operation and temperatures remain inside
normal parameters. I was happy to find CHTs remaining at 317-376 even with
the mixture leaned.
Even as the Outside temp
approached 91F, the oil temp remained at 218-219F. I decided to continue
with the Protocol 4 test card, which consists of testing the lending gear with
both the electric and manual controls while noting any flight changes. The
most noticeable change was an increase in both oil temps (from 218-226F) and an
increase in CHTs to the 360-395F range. After retracting the gear again,
the temps reduced almost back to previous, although oil temp stay about
220-221F.
There was one other temp that was getting a little high...the pilot. The
GRT was reporting cabin temp of 121F as I tried to adjust the vents to keep me
cool. At that point it had been about an hour and I decided it was time
for me to seek out air conditioning. I brought the plane back down, and
taxied back to the hangar. Oil temps climbed to 233F during taxi, but
that's pretty normal for a pusher on a hot day.
One other 'test' we're still working on is the camcorder mount. Fiberglass
aircraft are very rigid and thus transmit engine vibrations very well. We
attempted to use a foam isolator on the camcorder mount this flight, but the
foam was too thin and soft to provide much isolation once the camera was
tightened to the mount. Christine did get some good photos from the ground
though.
