Engine Rebuild

Start:  05/30/09
Finish:
Total Time: 75 Hours

This isn't something covered by the plans, so while it relates to chapter 23, we felt it best to separate this task out.  The engine we purchased had over 2800 hours on it since it's last overhaul.  Considering the recommended Time Between Overhaul (TBO) from Lycoming is 2000 hours, we knew when we bought it that we'd have to rebuild it before flying with it.

The plans suggest finding a mid-time engine that is proper working order so that one isn't proving out an engine at the same time as the airframe.  This is great advice, and had we found a mid time C1C when we needed to purchase we would have used one.  Rebuilding will give us a better understanding of the engine though.

After removing the engine from the airframe when we were done with fitment, the first step was to disassemble the engine for cleaning and measurement.

We found a number of cracks in the crankcase after we got the sump and the cylinders removed.  While we're aware that crankcase cracks are not uncommon, we're not familiar enough with these engines to determine which cracks can be repaired, and which, if any, are cause for discarding the case.  We'll leave that determination to the experts at the engine shop.  We're not particularly worried at this point though, as the business we purchased the engine from is reputable and guarantees the cases and crankshafts to make overhaul.  Swapping out the case would only take a quick lunch hour errand.

As suspected, the extensive cracking in the crankcase was cause to reject it.  It could not be repaired, so new crankcase halves were required.  Wentworth Aircraft, where we purchased the engine, found suitable replacements, and delivered them to Bolduc Aviation (our chosen machine shop).  The new case was inspected, found serviceable, and cleaned.

The crankshaft was also inspected, found to be in great condition, requiring only minor polishing (no undersizing of bearing surfaces would be required).  The AD for the crankshaft gear was performed, and the rods were reconditioned and reassembled onto the crankshaft.  The IO-360 rod bolts are tightened to length, not torqued to spec, and this is not a procedure we were familiar with, so we had Bolduc perform this step.

Our first step in reassembling the crankcase (after finishing the cleaning and inspection of all parts), was to get the one piece oil seal installed behind the prop flange.  This sounds simple enough, but stretching it over the flange requires a lot of grease, both elbow and conventional.

The bearing surfaces are then lubricated and the crankcase mating surfaces are prepared for joining with anaerobic sealant and silk thread.  The two piece front bearing on our IO-360 requires care be taken to mark the alignment of the bearing in the case, when installed into the dowels for it.  With the crankcase assembled on the engine stand, we can now install the cylinder assemblies, and the accessory housing.

With the major assemblies together, we painted the engine.  The color scheme we decided on for our engine is blue with black accents.  It might be a bit much blue, but overall, we like it.  With most of the engine assembly complete (just need a new fuel pump and an ignition system at this point), we're about ready to bring it to Bolduc Aviation to be run in on a test cell.

After installing a new fuel pump, and procuring the ElectroAir ignition systems we transported the engine (including the GRT engine monitor) back to Bolduc for initial run in.  Video from its run in can be seen here.

We had two minor issues to deal with after run in.  First, the map sensor on the secondary ignition control unit (which was purchased used) was malfunctioning, causing that unit to lag the primary by 6-8 degrees.  The engine still ran fine, but was about 50-70 rpm below the peak we were expecting.  Second, my 'guess' at the midway point on the oil pressure regulator setting about a turn too low, causing our peak warm oil pressure to be about 68-70psi or about 10psi low.

Aside from that, run in went very well.  Peak CHTs never passed 370 deg, and peak oil temp was 172deg.  After a couple hours of run in we drained the oil, ad cut open the filter.  Both were very clean, and we deamed the engine fit for flight.